Our Approach
Drilling Automation
Drilling Outcomes
About H&P
H&P Saves Operator 9+ days
First 10,000 ft U-Turn Well in Haynesville Basin
AUTOMATED HIGH TORQUE WRENCH LEADS TO 60% LESS DEFORMATION WHEN APPLYING FORCE TO DRILLPIPE
DrillScan® Technology West Africa Case Study
Removal of one casing string from well architecture saved tullow oil $4M USD per well
StallAssist® software prolongs life of weak motor to avoid unplanned trip
DrillScan® Software Identifies Drilling Dysfunction Causes in Complex, Multilateral ERD Well
By Working with the Operator, H&P Reduced the Average Curve Time by 3 Hours
Automated, Real-Time Forward Monitoring Outperforms Traditional Mathematical Projections
By Mitigating Motor Failures and the Associated Time Lost, Operator Saved $105,000 Per Well
Next-Level Drilling Automation Lowers Drilling Costs and Results in Better Hydrocarbon Production Potential
Operator Saves 2.38 Days of Drilling Time, Equating to a Savings of Over $140,000 Per Well
Adding Value Through Automation
Operator Utilizes Survey Management to Help Ensure Accurate Survey Data
Comprehensive Solution Increases ROP While Drilling And Maximizes Footage To Boost Production
Integrated Drilling Solutions Break Records While Reducing Operator's Time To Target
Permian Basin Operator Achieves 15% Higher ROP And 21% Improvement In Back To Drilling Time
61% Average ROP Improvement Reduces Operator's Time To Target
Operator Increases Rotating ROP, Enhances Bit and BHA Integrity with FlexDrill® Technology
Texas Operator Sees An Average Savings Of $42,000 At $70,000 Spread Rate
Midland Operator Increases Footage per day by Almost 94% & Enhances BHA Reliability
H&P’s Bit Guidance System® Saves an Average of $70,000 per Well
Oklahoma Operator Enhances Bit and BHA Integrity, Reduces Failure and Repair Costs with FlexTorque® system
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Let us prove why we'vebeen an industry leaderfor more than 100 years.